Paveltolz
Доверяй, но проверяй
Built a list of things to do post trip and, after getting postponed yesterday rescuing the Spousal Unit (flat tire), I started in on it today.
Not Truck related was getting the lawn mowed early since it was in need before we left two weeks ago.
Jacked up the back, drained the gear oil. Checked the magnet and there’s was a little material collected but, very fine and its been too long between changes. Needed another quart of oil but, spousal unit is gone with her car and so I moved to another task.
While playing mechanic trying to swap in a starter correctly at BigT’s I noticed the number 4 glow plug wire wasn’t attached to the GP and the ceramic fitting had melted (WT…). When I checked it today, it was connected and I could see it was repaired. BigT’s mechanic apparently noticed it and corrected it while he was in there un-screwing my mistake on the starter. Never said anything and didn’t charge me for it. Awesome.
Driver’s side Half-Shaft replacement time after that. Pulled the hub stub I inserted to keep things together while we continued the trip and then got the ‘cup’ off the differential. Expecting a wrestling match getting in the new unit, it went in easily…too easily it would seem but, no breaks in the differential so, accept the blessing and go on. What caused it to fail in the first place is a mystery to me but, I did order the bump stops and will get on that task when they show up.
Then the postman dropped off the new door pins and bushings from Cunningham Machine. Been watching YouTube vids on how to do the job and will try to work up the nerve since it’s the wife who will have to steady the door.
Not Truck related was getting the lawn mowed early since it was in need before we left two weeks ago.
Jacked up the back, drained the gear oil. Checked the magnet and there’s was a little material collected but, very fine and its been too long between changes. Needed another quart of oil but, spousal unit is gone with her car and so I moved to another task.
While playing mechanic trying to swap in a starter correctly at BigT’s I noticed the number 4 glow plug wire wasn’t attached to the GP and the ceramic fitting had melted (WT…). When I checked it today, it was connected and I could see it was repaired. BigT’s mechanic apparently noticed it and corrected it while he was in there un-screwing my mistake on the starter. Never said anything and didn’t charge me for it. Awesome.
Driver’s side Half-Shaft replacement time after that. Pulled the hub stub I inserted to keep things together while we continued the trip and then got the ‘cup’ off the differential. Expecting a wrestling match getting in the new unit, it went in easily…too easily it would seem but, no breaks in the differential so, accept the blessing and go on. What caused it to fail in the first place is a mystery to me but, I did order the bump stops and will get on that task when they show up.
Then the postman dropped off the new door pins and bushings from Cunningham Machine. Been watching YouTube vids on how to do the job and will try to work up the nerve since it’s the wife who will have to steady the door.