Nessmuk
Well-Known Member
1500 miles round trip. First day was a pip. Oil loss and massive blue smoke. Unplugged the CDR and been good since. Maybe a quart used since. Ran the hose back by the heater fan. Ordered a new CDR.
-Power steering / hydro boost is an issue. Pump overflows when braking until the pump is half empty. Is it likely the hydro boost?
Next issue,
-I get white smoke when into the turbo. Boost maxes at 10psi. Egts @ 1100 absolute max. Do I need to advance the pump?
Next issue,
-It has 5 psi fuel pressure at full boost on the passenger tank. When running on the drivers tank, it is zero. Same pump and filters. Wouldn't that be the fuel sock or a kinked line?
For a truck running on Rotella and STP to get oil pressure, and a hurried pump and turbo install, it did ok. 45 mph up a lot of the I-81 grades pulling a long, heavy trailer.
Found my WMI pump was frozen up. Every bearing in it was rusted solid. Ordered another and I'll put it in a cover.
Every time that steering over flowed, it looked like Cheech and Chong in the cab. Drafts in places I didn't know of. Took 3 days to get there. Lots of stops, changes, checks, fresh air and sleep.
Coming back I lost about 4 hours in traffic. A tractor trailer and then a two car accident.
At least I wasn't pulling the trailer at that point.
I'm still in Virginia at this point. Another day to go before I can tune on it.
-Power steering / hydro boost is an issue. Pump overflows when braking until the pump is half empty. Is it likely the hydro boost?
Next issue,
-I get white smoke when into the turbo. Boost maxes at 10psi. Egts @ 1100 absolute max. Do I need to advance the pump?
Next issue,
-It has 5 psi fuel pressure at full boost on the passenger tank. When running on the drivers tank, it is zero. Same pump and filters. Wouldn't that be the fuel sock or a kinked line?
For a truck running on Rotella and STP to get oil pressure, and a hurried pump and turbo install, it did ok. 45 mph up a lot of the I-81 grades pulling a long, heavy trailer.
Found my WMI pump was frozen up. Every bearing in it was rusted solid. Ordered another and I'll put it in a cover.
Every time that steering over flowed, it looked like Cheech and Chong in the cab. Drafts in places I didn't know of. Took 3 days to get there. Lots of stops, changes, checks, fresh air and sleep.
Coming back I lost about 4 hours in traffic. A tractor trailer and then a two car accident.
At least I wasn't pulling the trailer at that point.
I'm still in Virginia at this point. Another day to go before I can tune on it.