I'm leaving the "silent majority" to actually participate in the forums. The 6.5 community here is great, and discussion / knowledge sharing betters every build. I'll post pics of my 6.5TD/GMT400 project work under the appropriate topics so others can provide feedback or get inspired. Disclaimer: I'm Canadian. Expect metric!
I'm a mechanically inclined Civil Engineering Technologist, the GMT400 & 6.5 has been my gateway to DIY diesel mechanics.
My 8+ year DD project is a Burgundy 1997.5 GMC K1500 Ext cab short box with the 6.5 TD. Preventative maintenance and weakest link upgrades on the go since day one.
First motor went when I blew a stock oil hose at 260KKm. I had done the double screw clamp and wire tie mod suggested in TDP Volume I book, but the failure was through the sidewall of the rubber about midway down the hose. Should have just went with braided steel and that's what I go with now.
Second motor was from a '95 GMC 2500LD parts truck. Didn't believe the seller when he said it had a rebuild HMVW block with 80KKm, I didn't know there was a difference at the time or how to check but he accepted my lowball offer.
In March I pulled the second motor at 340KKm after the #6 nylon intake rocker retainer failed. Threw smoke and imbalance DTC. The rings obviously failed in that cylinder. Fresh oil lined the #6 combustion chamber, passenger exhaust manifold, turbine housing, and tailpipe.
Recently discovered the ♦ stamp and "01 18 P" date. Meaning I have a 2008 Optimizer 6500 casting! It also had a girdle, timing gear, and updated DS4. I was going to just buy OEM rebuild kit then put it back together. Now that I know I have a Navistar block I will bomb proof the thing and build a solid highway commuter. Whatever reliable power I can get without blowing a head gasket is what I'll go for. Will likely try propane to get economy and make power if I peak out the DS4.
Here is my build & immediate plans at the time of writing. I'll update my signature line as things progress.
1997.5 K1500 6.5TD Highway Commuter:
Current Mods: '08 Navistar Block, ♦ Precups, DSG girdle, 4" wrapped SS exhaust, HX35W, Vac/EGR delete, F intake/plenum, Walbro + FTB fuel mod, Heath 80HP PCM, Boost/EGT gauges, #9, PMD relocate, Braided steel oil lines, dual alt's, G4D batteries, 4/0 cables, gear reduction starter, bosch glow plugs + PT wire upgrade.
In Progress: Marine 18:1 Pistons, ARP head studs, LB7 Rad + Intercooler + Fan, '00 Balanced Water Pump & Clutch, single T-stat downgrade, Poly Mounts, 1/4" SS riveted rocker retainers w. fat washers (a nylon one failed on me).
Future: Banks OBS Exhaust Manifold + 2.5" Crossover + left header, Exhaust pressure gauge, Heath cam, Steel crank, Gapless 2nd rings, Peninsular intake.
Wishlist: Machined 1-piece bedplate, Ceramic coated chamber & exhaust, Port matching, Marine Injectors.
I'm a mechanically inclined Civil Engineering Technologist, the GMT400 & 6.5 has been my gateway to DIY diesel mechanics.
My 8+ year DD project is a Burgundy 1997.5 GMC K1500 Ext cab short box with the 6.5 TD. Preventative maintenance and weakest link upgrades on the go since day one.
First motor went when I blew a stock oil hose at 260KKm. I had done the double screw clamp and wire tie mod suggested in TDP Volume I book, but the failure was through the sidewall of the rubber about midway down the hose. Should have just went with braided steel and that's what I go with now.
Second motor was from a '95 GMC 2500LD parts truck. Didn't believe the seller when he said it had a rebuild HMVW block with 80KKm, I didn't know there was a difference at the time or how to check but he accepted my lowball offer.
In March I pulled the second motor at 340KKm after the #6 nylon intake rocker retainer failed. Threw smoke and imbalance DTC. The rings obviously failed in that cylinder. Fresh oil lined the #6 combustion chamber, passenger exhaust manifold, turbine housing, and tailpipe.
Recently discovered the ♦ stamp and "01 18 P" date. Meaning I have a 2008 Optimizer 6500 casting! It also had a girdle, timing gear, and updated DS4. I was going to just buy OEM rebuild kit then put it back together. Now that I know I have a Navistar block I will bomb proof the thing and build a solid highway commuter. Whatever reliable power I can get without blowing a head gasket is what I'll go for. Will likely try propane to get economy and make power if I peak out the DS4.
Here is my build & immediate plans at the time of writing. I'll update my signature line as things progress.
1997.5 K1500 6.5TD Highway Commuter:
Current Mods: '08 Navistar Block, ♦ Precups, DSG girdle, 4" wrapped SS exhaust, HX35W, Vac/EGR delete, F intake/plenum, Walbro + FTB fuel mod, Heath 80HP PCM, Boost/EGT gauges, #9, PMD relocate, Braided steel oil lines, dual alt's, G4D batteries, 4/0 cables, gear reduction starter, bosch glow plugs + PT wire upgrade.
In Progress: Marine 18:1 Pistons, ARP head studs, LB7 Rad + Intercooler + Fan, '00 Balanced Water Pump & Clutch, single T-stat downgrade, Poly Mounts, 1/4" SS riveted rocker retainers w. fat washers (a nylon one failed on me).
Future: Banks OBS Exhaust Manifold + 2.5" Crossover + left header, Exhaust pressure gauge, Heath cam, Steel crank, Gapless 2nd rings, Peninsular intake.
Wishlist: Machined 1-piece bedplate, Ceramic coated chamber & exhaust, Port matching, Marine Injectors.
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