I figured I would post an update....
Well today on my black 93 truck I did what I didn't think I could do! I have been wanting to do something with the AC on it just to see what worked and what would need to be done just to have it function. I know it all needs to be replaced and gone through but I got a stubborn hair up my rear today!!
I ended up picking up a new AC dryer, orifice tube, clutch cycle switch, some pag-100 oil, and 4 cans of 134A. started tearing things down to flush, pulled the front grille off and went at removing the old orifice tube. the line coming out of the condenser was bent in two places. I managed to tweak the lower bend straight and finessed the other bend right where the threaded fitting was. Got it all straight enough to pull the old orifice. Once I got it out I noticed right away that it was not that bad. hardly any debris on it. when I went to flush it out, I first just blew through it with a rag covering the other side. nothing but air and a little oil came out which was clean oil!!
Now keep in mind this system has been open to the environment with the dryer missing since 2009. there are photos on the forum showing this.
Next I flushed the evaporator out, then went to clean out the hoses connected to the compressor. This is when I found the show stopper... the high side hose was blown out right behind the compressor!
well in a pinch I decided to run out to the local pick a part yard and see if I could find one still in tact. To my dismay every truck I found, the hoses were all cut with a knife. I soon realized that this JY was slicing the hoses as the vehicles were coming into the yard instead of recovering the refrigerants. I was about to give up when I found myself standing over a burb in the JY that had rear air. I noticed where the hose coming off the compressor manifold going to the rear was cut but the other two for the front unit was still intact.
on a whim I thought to myself, the low side only ever sees about 150 to 175 PSI when the AC is off. and I could easily plug off this extra port on the manifold and possibly use it to see what this trucks AC will do. $25 later I was on my way home with the hose LOL
Got home and got everything cobbled up. ended up using a piece of copper tubing with one end I brazed shut clamped in to plug off that hose that was for the rear air. started vacuuming it down... it held. then I thought pressurize the system with my air compressor just to see if anything leaked before wasting any cans of 134a. I pressurized it up to about 80 psi and let it sit there a while. got a spray bottle with soap and went to town on it, but only found a small leak on the high side service port. I ended up just putting the cap on it and said it's good enough I will know if this thing will work or if it's gonna explode.
added the 8 oz bottle of pag-100 oil in the dryer, some in the hose, and some directly in the compressor while rotating the clutch by hand. closed up the system for the last time and pulled a vacuum. I finished off the night (11PM) with only charging it with about 30 oz of 134a so it's a little low yet but with the blower on high I was seeing a hair under 50 degrees on the thermometer. I let it run for a while and then put the blower on medium. came back and the temp was showing right at 40 degrees!!! The compressor is not making any noise ether.
This thing has not worked in at least 14 years, After seeing the ports on the compressor clean and not full of black chalk like they normally are along with the oil that came out of the condenser clean. I am suspecting this system was working long ago when the high side hose let go and then was never fixed.
I will check it again tomorrow and possibly give it a full charge if it holds over night, but I'm in shock it actually worked!!